| EYEWITNESS: "A/C 43-37521 was
attacked by an ME 262 at 1109 hours,5240N, 1200E and the left stabilizer
broke off. A/C was last seen going down into contrails under control
with E/A making another attack. " On 19 Sept. 1945 in Los Angeles, CA. , Rollie King gave the following
statement:
"I was the pilot of a B-17 type aircraft in which S/Sgt Robert G.
Mitchell was ball-turret gunner, and that on 17 March 1945 we
proceeded on a regularly assigned bombardment mission over Berlin.
That on said date,S/Sgt Mitchell was acting as ball turret
gunner. After bombs away on the target, we received numerous fighter
passes. The first fighter pass knocked out our vertical stabilizer
and the tail turret, killing the tail Gunner. On the next fighter
pass we received a great deal of damage to the plane and practically
all of the controls were knocked out.
I called back and had the radio operator check the crew members,
however I did not receive a reply as to their condition. On the
third fighter pass we received a burst near the front which knocked
out all of our controls and put the plane into a violent spin. I
ascertained that I was going to be unable to get the plane out of
the said spin due to the lack of control and I told everybody to
bail out.
S/Sgt Gitlin, he waist gunner, checked the ball turret gunner and
he had previously checked in the tail for the tail gunner. I saw
Sgt. Gitlin going out by himself and inasmuch as S/Sgt Robert G.
Mitchell was a very close friend of his, I do not believe he would
have bailed out if he could have in any way helped Sgt Mitchell.
I have never seen Sgt. Gitlin since that time, nor have I heard
what happened to him,and I do not know whether or not his chute
opened when he bailed out.
I have never heard regarding S/Sgt Mitchell,and I do not know
whether or not his chute opened, or whether he bailed out, prior to
Sgt Gitlin. As soon as I bailed out the ship exploded. "
Rollie C. King
1st Lt. , Air Corps
Compare above with the following statement made by F/O John W.
Spencer at his home in Elizabethtown, KY on 3/11/45:
". . . . Am writing in response to a letter received by me today
considering S/Sgt Robert G. Mitchell. The last time I actually saw
Sgt. Mitchell was on the ground before take-off 18 Mar. 1945 but he
was on the mission. Everything went well until just after we had
turned on the I. P. a couple of minutes after we turned we were hit
by an ME 262 that got practically all of the left horizon-
stabilizer. A second attack was fought off half way down bomb run
with no damage done.
Since being hit we were gradually trailing the formation more and
more so by the time we were over the target area the rest of the
formation was approximately one-half mile away. We salvoed our bombs
over the "built up" area at 1125 and at approximately 15 to 30
seconds later there was a terrific burst that seemed to come from
the rear of the plane. From where I was in the nose I could see
smoke boiling up from under the pilot's seat.
The conditions of the plane then was that the controls had been
shot out, as had the Interphone system, & the right wing was on
fire. Up until we received this last attack everyone in the ship
reported they were all right. As soon as we were hit -since there
was no communication - I looked thru the astro-dome into the cockpit
& my first pilot nodded for me to bail out. So then I handed my
toggalier his chute & then put on my own but still wasn't sure to
bail out so looked thru the astro-dome again & seen both pilot &
co-pilot preparing to abandon ship. Then looking at the right wing
which was burning pretty badly decided it was time to leave. So I
bailed out, floated to the ground and was picked up immediately.
The rest of my information was received from talking to the
fellow crew members when I ran into them two or three days later. I
found out that ourtail gunner, James D. Baker, was hit badly on the
last attack - or may even have been killed & never left the ship.
Later on his unopened, bloody, chute was shown to the enlisted men
of the crew & they recognized the number on it to be his.
As to Mitchell, his fate is not known. The crew member who was to
assist him out of the ball turret - in case of emergency -is also
missing -waist gunner Meyer Gitlin. Altho the waist gunner is known
to have bailed out, he was not seen since. The radio operator,
Archie M athosian,says that Gitlin bailed out ahead of him through a
hole in the fuselage made by cannon shell from the jet. From that
time to my knowledge he has never been seen or heard from.
It is my suspicion that,if his chute did open he may have been
killed by the Germans for he was a Jew,had it on his dog tags, and
didn't seem to care who knew it. That may or may not have happened.
Nonetheless that was the last seen of him. If he were alive today he
could probably tell what happened to Mitchell.
According to my talks with the crew no one knows what condition
the ball turret was when the last man abandoned ship. The only other
man in the rear of the ship was the radio operator and since he says
he does not know I know of no way of finding out.
Spencer ends his letter with a list on names of crew and their
addresses.
Crew Members of B-17 "Heavenly Days"
351st Sqdn. 100th Bomb Group
43 38861
351st Squadron.
Crew joined 100th on 5 Oct 44. |
|
SGT WILLIAM
C. DANIELSON, JR.
(KIA 18 MAR 45) |
ROG |
2ND LT
EDWARD P. GWIN
(KIA 18 MAR 45) |
P |
SGT HERBERT
HAMANN
(POW 18 MAR 45) |
TTE |
2ND LT
DONALD H. REICHEL
(POW 18 MAR 45) |
CP |
SGT Earl S.
HAMILTON
(grounded at some point) |
BTG |
2ND LT
ROBERT B. LANDINO
(POW 18 MAR 45) |
NAV |
SGT NORMAN
D. HEILBUTH
(POW 18 MAR 45) |
WG |
| 2ND LT
STEWART P. LAIDLAW |
BOM |
SGT CHARLES
T. MAEDEL
(NOC) |
WG |
| |
|
SGT JOSEPH
M. GRIEGO
(POW 18 MAR 45) |
TG |
Letter from Joe Griego in 1983 states that Lt. Laidlaw was made Group
Bombardier after about 10 missions with crew. "On 18/3/45 Sgt Raymond
Y. Uhler and Sgt John W. Disher were flying in place of Hamilton &
Maedel and both were KIA. Sgt. David Ackerman was aboard as NG and
became a POW. R. K. Uhler was from the crew of J. L. Wofford. John
Disher was from the crew of H. S. Bucklew. S/Sgt N. D. Heilburth was
aboard as a waist gunner and became a POW. "
MACR #13144 A//C#43 38861 was attacked by an ME 262 at 1114 hours,
5247;N & 1145E.
Our A/C had two engines on fire and dived away from the formation. .
A/C then nosed up with tail falling off and fell down spinning. One
chute was seen. "
Joe Griego was in the severed section of the tail and had a difficult
time getting out so that he could open his chute.
See S. O. C. p. 86/87 &103/105
The following are excerpts from statements of Lt. Robert B. Landino
taken from MACR No# 13144
As to Lt. Gwin, ". . . from enlisted men who were working near
where we were shot down; they claim one man bailed out below the clouds,
then they heard shooting, his chute collapsed and he fell to the ground
presumably dead. "
As to Sgt Disher, " . . . S/Sgt Heilbuth saw him just before he
bailed out. He was crawling out of the radio room with blood all over
himself, but he (Heilbuth) did not have time to help him as the aircraft
was below the clouds which were not more than 500 feet, so he had to
jump. Disher probably never got to the door to jump as the plane must
have hit only a few seconds later. "
As to Sgt. Uhler, ". . . I believe he was trapped in the ball
turret by enemy shell fire. His body was seen on the ground along side
of the plane. "
As to T/Sgt Danielson, ". . . He must have been killed by the fire
from the two ME - 262s that shot us down. They sprayed the back part of
our plane as it was shot in half just in front of the tail wheel. "
44-8717 418th Squadron.
Crew joined the 100th on 24 Dec 44 |
|
T/SGT
ROBERT A. HAUSAM
(POW 18 MAR 45) |
ROG |
CAPT ROGER
L. SWAIN
(POW 18 MAR 45) |
Com P |
T/SGTMORRIS
O. KOLLING
(KIA 18 MAR 45) |
TTE |
1ST LT PAUL
E. DE WEERDT
(POW 18 MAR 45) |
P |
S/SGT
NORBERT J. DOUGHERT
(REPLACED BY RADAR NAV) |
BTG |
F/O JAMES
M. CARDEN
(POW 18 MAR 45) |
NAV |
S/SGT PETE
J. FISCHER
(POW 18 MAR 45) |
WG |
2ND LT
BERNARD F. KOZIK
(POW 18 MAR 45) |
BOM |
2ND LT BILL
E. THOMPSON (CP)
(POW 18 MAR 45) |
TG |
F/O SUMMER
H. WOODROW
(POW 18 MAR 45) |
Radar N |
|
|
On the 18 Mar 44 (Berlin) mission Capt Roger L. Swain was flying as
Command Pilot and became a POW. F/O Summer H. Woodrow, a Radar
Navigator, flew instead of Norbert Dougherty and became a POW. Bill E.
Thompson, the regular CP flew in the TG position for this mission. See
Thompson Memo for a description of the attack, his bail out and POW
experiences. . . . . pw
(BILL THOMPSON BELIEVES MORRIS KOLLING WOULD NOT LEAVE THE AIRCRAFT
AND PAUL DeWEERDT WOULD NOT BAIL OUT WITH KOLLING STILL ABOARD AND ONLY
SURVIVED BECAUSE HE WAS BLOWN CLEAR OF THE AIRCRAFT WHEN IT EXPLODED
SEVERAL MINUTES AFTER THE BAIL OUT ORDER WAS ISSUED. )
According to statements in the MACR, T/Sgt Morris O. Kolling had
flown a tour in the CBI (China - Burma - India) theater and had a total
of forty (40) to fifty (50) missions. After Capt. Swain bailed out,
Kolling took over his seat - DeWeerdt thought Kolling to be in dazed
condition and would not bail out. Aircraft was probably hit again and
went into a spin and DeWeerdt got out some way. (May have been blown out
in an explosion) DeWeerdt was later shown Kolling's wallet by the
Germans and told that a body was found in the co-pilot's seat.
44-6295 351st Squadron.
Crew joined the 100th on 21 Jan 45 |
|
SGT JOHN T.
PALMER |
ROG |
|
LT MERRILL E. JENSEN |
P |
SGT THOMAS L. GALLAGHER |
TTE |
|
F/O CHARLES L. KEMP |
CP |
SGT HOWARD B. HODGES |
BTG |
|
F/O RICHARD R. SCROXTON |
NAV |
SGT ANTHONY G. SCHEMBRI |
WG |
|
SGT CHARLES P. FRIEL |
NG |
SGT MELVIN J. MADSEN |
TG |
This crew flying its 14th mission, took off for Berlin 18 Mar 1945.
In a letter of Nov. 1983 Richard Scroxton relates what occurred:
"We were in the #3 position slightly behind and below the element
lead. As we neared our target of Berlin, he sky was clear but we
were leaving heavy contrails. There had been no warning of bandits
when our tail gunner opened fire. Four M~ 262s came in hidden by the
contrails and hit four of us. I had one quick glance of ours just
off our left wing tip which was then five feet too short. Our
element lead was also hit and turned directly into us we turned in
formation and he slipped below us.
This change in position was not noted by the person who wrote the
report as it applied to the other plane. (He is here referring to a
report of an eyewitness who had said that Scroxton's a/c had the
entire left wing afire and that two men Were seen to jump from the
ship. jb) No one bailed out of our plane partly because several
chutes were destroyed. In addition to the wingtip damage, 4 engine
prop was hit resulting in very severe vibrations. These and other
hits on #2 and #3 made it clear that we were no longer a part of the
formation. I gave the pilot a heading of due East we crossed the
Oder river front line at 9,000 ft down from 33,000. At 2,000 ft. we
were able to maintain altitude and picked an open field
We did take one very close flak burst that ripped up the chutes
near the front escape hatch. We landed near a town in Poland called
Kostian. We thought that our troubles were over when we landed gave
away all our provisions even those in the raft. We spent that day
and next with Russians then they put us on our own. We traveled by
horse cart, railroad flat car, etc. until we got to Lodz. There we
met a crew with a C47 who had flown in to evacuate an injured airman
it turned out to be Capt. Ernst of the 100th. (Ernst had flown as
pilot of a mission on 3/2/45 Robt. Rosenthal Command pilot and
suffered a wound which caused amputation of his leg. jb)
We flew with him to Poltava. Melvin Madsen had left us in Poland
due to sickness but he got back to the States before we got back to
England. As we got off the plane in Poltava, I saw a classmate from
Navigation school who had arrived the day before and left the next
day. We expected to do the same but the Russians had other ideas. We
were not allowed to leave or write for four weeks. We left Poltava
on April 23 in a B 17 with another crew. We landed in Bari, Italy
dropping off the other crew then flew to Caserta and stayed two days
then flew back to England landing at Thorpe Abbotts on 25 April
1945. "
Mar 19, 1945
Tactical Report from the 13th Combat Wing reports that the primary
target was Lutzendorf but weather conditions forced the formation to
attack the Carl Ziess Optical works at Jena, Germany. The 100th
dispatched 34 aircraft plus 4 PFF and all but one attacked. One aircraft
was forced to return early with total oxygen system failure. There were
no losses on the mission, but the 100th received the bitter news that
Major Summer Reeder was lost on a C-54 training flight in Florida.
Reeder was original 100th and had completed his tour before the advent
of effective fighter escort. The popular and highly respected Reeder won
the DSC on the September 6, 1943 Stuttgart mission when he had brought
the crew home with the Harry Edeburn, the co-pilot dead, and himself
wounded. Summer Reeder's loss was a grievous one for the 1900th.
Navigation reports the route flown to be essentially as briefed to
control Point #1. Enroute to the Pre-IP, 13A was 6 - 7 miles right of
course while in the bomber stream. A course correction was made and the
Pre-IP was made good. Bombing altitude (25,500 feet) was reached 10
minutes prior to the IP. The IP was made good by 13A and B. 13 A peeled
off for individual H2X runs. Bombing results were considered
disappointing.
Weather: A low stratocumulus layer prevailed over the base area and
enroute to the Continental assembly area. In the assembly area patchy
middle clouds were encountered at 12,000 feet, but cause no difficulty
with the assembly. The IP was visual but there were contrails and cirrus
clouds to 25,000 feet on the bomb run and to the Rally Point.
Mar 20, 1945 No air activity - stood down
Mar 21, 1945
Tactical Report from the 13th Combat Wing reports that the 13A group
made up of the 100th A, B, & C took-off for Ruhland, led by Colonel D.
L. "Handlebar Hank" Lyster. Weather forced Lyster to divert and attack
the secondary, the machine shops one and on-half miles southwest of
Plauen, Germany. The Lead Bombardier had some problems with the Norton
sight, never-the-less he hit the tank factory and machine works dead on.
All but three aircraft attacked the target and there was one aircraft
lost to ME-262 jet fighters. A/C #44-8613 was destroyed by the jet
fighters on the bomb run. The crew was as follows:
44-8613 350th Squadron
Crew joined the 100th on 4 Feb 45.
|
|
Crew was on their 14th or 15th mission. MACR
#13572, Microfiche #4952 |
|
2ND LT
BERNARD L. PAINTER
(POW 21 Mar 45) |
P |
SGT ARTHUR
B. MAC NEIL
(KIA 21 Mar 45) |
ROG |
2ND LT
CHARLES W. HIGGINBOTHAM
(KIA 21 Mar 45) |
CP |
S/SGTVIRGIL
S. DOWNING, JR.
(KIA 21 Mar 45) |
TTE |
F/O DANIEL
MARTIN
(KIA 21 Mar 45) |
NAV |
SGT WALLACE
R. MATZDORF
(KIA 21 Mar 45) |
BTG |
S/SGTHERBERT SINGER
(KIA 21 Mar 45) |
TOG |
SGT EMIL E.
HAVELKA
(KIA 21 Mar 45) |
WG |
| |
|
SGT DONALD
A. BECKER
(KIA 21 Mar 45) |
TG |
EYEWITNESS: "100TH "A" was attacked by five (5) ME 262's at 0940
hours at 51°33"N & 13°41"E. Aircraft 44-8613 which was straggling with
another aircraft two (2) miles behind the formation was observed to be
hit in the left wing. It exploded and went down in tight spin. Three (3)
chutes were seen, two of which reported to be on fire. "
The following letter was written by Bernard Painter and appears in
the MACR file.
Subject: WHEREABOUTS OF CREW MEMBERSJune 23, 1945
TO: Major Wm. D. Sanders
SIR: In answer to you request for information concerning the
whereabouts of the missing airmen I will give you what details I have.
We were scheduled to bomb Ruhland, Germany on March 21, 1945. Fifteen
(15) minutes before the target we lost N0#1 engine due to a mechanical
failure (Supercharger). We were forced to leave the formation and to
salvo our bombs. We accomplished this and were rejoining the formation
when attacked by several ME 262 Jet Fighter planes. Although our gunners
were firing at them constantly, they were able to shoot out #2 engine
and set it on fire, foul the controls rendering them useless and scored
several hits in the nose section, setting it on fire.
I immediately gave the order to abandon ship and went below to aid
the men in the nose, but was unable to accomplish this because of the
fire and was forced to bail out at approximately 18,000 feet. I opened
my chute immediately in an effort to drift toward the Russian lines. I
counted five (5) chutes below me and I can presume they were crew
members from the rear of the ship who jumped when we were at 22,500 and
made a delayed jump.
I have had no contact with the crew since that time. I have written
all of the next of kin and given them what I could of the above details.
I will also try to call on many of them personally. I would appreciate
any information you receive concerning the missing men forwarded to me
and I will do likewise with any received through other airmen. "
Bernard Painter
1st Lt AR 0-926819
Box 327 Carlinsville, IL.
The navigation section of the report indicates the briefed route was
closely followed to the IP for the primary target. At this point a
southerly heading was taken, skirting the Chemitz flak concentration, to
the IP for the secondary. The bombing altitude was not made good because
of cirrus clouds at 24,000 feet. 13A bombed in group formation due to
the presence of fighters in the area.
The weather in the secondary target area was 8 to 9/10 cirrus at
24,000 feet. The target was clear with a downward visibility of 15 - 20
miles.
Bombing: The primary was not attacked due to the undercast. After
making an IP at 50°30"N & 13°18"E, the bombardier took over. Six minutes
from the BRL (bomb release line) the bombardier identified the assigned
AP and proceeded to synchronize. Immediately after synchronization
began, the formation encountered prop wash and the bombardier
experienced a tumbled gyro, this occurred again and during the little
time left the bombardier resynchronized using a caged gyro. At bombs
away synchronization was excellent and bubbles level. Because of the
presence of enemy fighters bombing was in Group formation at 21,000
feet. Bombing results were excellent, the target being hit squarely by
the 100th. They were declared EXCELLENT
Mar 22, 1945
The 100th took-off at 0830 hours for the airfield at Alhorn and
dropped their bombs at 1130 hours from an altitude of 18,000 feet. All
but one aircraft attacked the target, bombing results were excellent,
and there were no losses.
The 13th Combat Wing Tactical Report relays that 35 aircraft plus 3
PFF were dispatched.
Navigation: The route was flown essentially as briefed to the Pre-IP.
At this point 13B and 13C were to the right of course in order to obtain
the proper interval and approach to the IP. Bombing altitude was reached
45 minutes prior to the IP. The IP was made good and individual visual
runs were made on the primary target.
Weather: Enroute a haze layer prevailed with the tops at 10,000 and
nil to 3/10 cirrus clouds above 25,000 feet. The target area was clear
with visibility 15 to 20 miles in haze.
Bombing: After the maneuver at the IP, which was made good, the
bombardier took over and proceeded to kill course, using the extended
vision. 17 miles from the BRL the bombardier identified the MPI and made
a well synchronized run of 4 to 5 minutes. When the bombs were released
on a true heading of 300°, synchronization was good and the bubbles were
level. C-1 Auto-Pilot was used on the bomb run. The photo reports
indicated the bombing of the 100th was declared GOOD.
Mar 23, 1945
The 100th, led by Colonel Fred Sutterlin, the Group Commander
attacked Unna with good results. The two Lead Navigators Carl Roesel and
Robert Kirby obtained solid hits on the marshaling yards with 100th A &
C, while the 100th A, with Tony Shiurba the lead navigator attacked the
last resort target at Marburg. This was due to the extensive smoke at
the primary from the Groups A & C squadron's bombs. Of the 34 plus 4 PFF
aircraft dispatched all attacked and one #43-37812 was lost. This A/C
was hit by flak and collided with a aircraft (#42-97812) flown by the
Laurance Lazzari crew, crinkling eight feet of his wing. At the time of
the collision the Lazzari plane was being flown by the co-pilot, Guiher
(Gene) Greenwood, who made a recovery and was escorted back to Thorpe
Abbotts by a flight of P-51's. Upon arriving at Thorpe Abbotts the
operations people were fearful the wing would collapse on landing thus
blocking the active runway. In view of this the crew was advised by the
tower to use one of the secondary runways. Interesting in the fog of war
is the fact that as they were on approach they were cut out by a B-25
with an engine on fire. Lazzari and Greenwood were able to abort their
approach and watched as the Mitchell crashed short of the runway but did
not explode or burn. The pilots, having enough of the emergency by now
elected to land on the long runway and did so safely.
(The fact these two aircraft had the same last three tail numbers has
confused historians for the last half century. . pw)
43-37812
351st Squadron
Crew joined the 100th on 9 Jan 45 |
|
SGT HOWARD
R. TUDOR
(KIA 23 Mar 45) |
ROG |
2NDLT
ALFONSO C. GUARDINO
(KIA 23 Mar 45) |
P |
SGT HUGH H.
PENNOCK
(KIA 23 Mar 45) |
TTE |
2ND LT
WILLIAM E. DAVIS
(KIA 23 Mar 45) |
CP |
SGT ALOIS
CHUDY
(KIA 23 Mar 45) |
BTG |
2ND LT LEO
TOMASO
(KIA 23 Mar 45) |
NAV |
SGT LEON K.
WILLIAMS
(KIA 23 Mar 45) |
WG |
SGT EDWARD
W. KEEFREY, JR.
(KIA 23 Mar 45) |
TOG |
SGT OBIE
SMITHART
(KIA 23 Mar 45) |
TG |
EYEWITNESS: "A/C #812 thought to have been hit by flak at 1428 hours
5034N 0745E. The right wing crumpled and A/C went into a spin then
leveled off for a moment then went into another spin. A/C exploded on
impact. No fire or smoke seen. No chutes seen. "
Guardino, Davis, Keefrey, Tudor and Chudy buried at Jefferson
Barracks, Mo. Probably this is a "common" grave. Smithhart buried in CA;
Pennock buried in Minn. ; Williams buried Pa.
MACR#l3604 Microfiche #4973
The 13th CBW Tactical Report
The 13A group was made up of the 100th's A, B, C, & D Squadrons.
Target: Primary - Unna, Germany.
Navigation: Bombing altitude was reached 40 minutes prior to the IP.
At the Pre-IP, proper interval was taken, and the peel off was made at
the IP for individual runs on the primary target. Since 100th D had not
released it's bombs they made a run on the 3rd priority target.
Weather was CAVU (clear and visibility unlimited) in the target area.
Bombing: After the maneuver at the IP, the bombardier took over and
proceeded to set up course. The attack was made on a true heading of
311°. The bombardier picked up the target area at 8 miles and identified
the assigned MPI (mean point of impact) one and one half miles from the
BRL (bomb release line). A normal sighting operation was completed and
bombs were released from 23,100 feet.
FI Report: The bombs from 100th A fell 500 to 1500 feet beyond the
MPI. A heavy concentration of bombs fell on the marshaling yards,
however, and all of the tracks were undoubtedly cut in several places.
About 25 goods wagons were smothered with bombs, and all of them should
be considered damaged or destroyed. Percent of the bombs within 1000 &
2000 feet of the MPI were 45% and 95%. Bombing results were declared
very good.
100th B bombs fell 1000 to 2000 feet left of the assigned MPI in
fields, scattered residences, and a highway. Percent of bombs within
1000 & 2000 feet of assigned MPI were 10% and 34%. Bombing results were
declared nil.
100th C bombs fell across the marshaling yards several hundred feet
left (west) of the assigned MPI. The heavy concentration cut all of the
tracks. Damage was inflicted on two small buildings inside the yard as
well. Bursts were visible in the smoke of 100th A's bombs and it should
be assumed additional damage was inflicted on the western portion of the
yard. Percentage of bombs within one and two thousand feet of the
assigned MPI were 90% and 97%. Bombing results were declared excellent.
100th D bombs fell on the northwest portion of the marshaling yards.
Two explosions occurred from direct hits on a goods wagon and building.
About fifteen of the visible bombs hit in the yards, probably damaging
at least 4 tracks in several places and approximately 12 - 15 goods
wagons. From 5 - 6 bombs hit in a residential area adjacent to the
tracks. The pattern of the bombs from only one aircraft are visible due
to smoke, the bombing results are thought to have been GOOD or better.
Mar 24, 1945
This was one of the few two missions days for the 100th. It was also
the day Allied forces crossed the Rhine river. On the 0600 hours mission
Major John Gibbons, who had came to the Group around ten mouths earlier
as a 2nd Lt. , led 34 100th planes and 4 PFF aircraft in attacks on the
airfield at Havelte in the Neatherlands. All of the aircraft attacked
and there were no losses. The returned at 1030 hours.
Shortly after noon Colonel Jack Wallace, destined to become the Group
Commander two and half months later, led the A, B, C, & D Squadrons of
the 100th as well as the 13th Combat Wing in an attack on the airfield
at Ziegenhain, Germany. All 34 of the 100th aircraft and 4 PFF ones
attacked the target and there were no losses although most of the crews
were exhausted.
Tactical Report from 13th CBW
13A Group = 100th A, B, C & D
Target: Airdrome at Zeigenhain, Germany, Primary
Aircraft Airborne: 34 and 4 PFF
Navigation: The route was flown essentially as briefed to the IP. The
Wing peeled off in squadrons on individual runs to the first priority
target.
Weather: CAVU conditions were prevalent throughout the mission. .
PFF Narrative: PFF equipment inoperative on 100th A and there was no
beacon received on 100th D.
Bombing: After the maneuver at the IP, which was made good, the
bombardier proceeded to set up course by pin-point pilotage. Ten miles
from the BRL the bombardier picked up the target area. With two minutes
for visual synchronization, the bombardier completed a normal sighing
operation. There was some difficulty identifying the assigned MPI. The
actual approach he used was slightly to the left of the assigned MPI.
C-1 Auto-Pilot was used on the bomb run at an altitude of 25,000 feet.
FI Report: The bombs from 100th A fell around the selected approach
which was approximately 1000 feet left of the assigned MPI. 3/4 of the
bombs dropped fell on the L/F. Percentage of bombs within 1000 and 2000
feet of the assigned MPI; 79% and 100%. Bombing results were declared
very good
100th B bombs fell 300 feet to the right of the MPI, all of them fell
on the L/F. The bombing results were declared as very good.
100th C bombs fell on and over the selected MPI, which was
approximately one half mile west of the assigned MPI. Practically all of
the bombs fell left or over the L/F. Percent of bombs within 1000 and
2000 feet of the AP: 70 % and 100%. Bombing results in relation to
damage inflicted on the target were declared as FAIR.
100th D bombs fell around the selected AP, which was approximately
one half mile west of the assigned MPI. Practically all of the bombs
fell on the L/F in the southwest corner. Percentage of bombs within 1000
and 2000 feet of the AP: 87% and 100%. Bombing results in relation to
damage inflicted on the target were declared as VERY GOOD.
Mar 25, 26, 27, 1945
There was no air operations, the Group stood down to rest and
recuperate from the heavy March mission schedule.
Mar 28, 1945
The 100th attacked the marshaling yard, this was the secondary target
the primary being a tank factory, at Hanover, Germany. There were no
looses and only one aircraft failed to attack the target, A/C # 817 was
forced to return after the loss of No #3 engine.
Tactical Report from 13th CBW
13A Group = 100th A, B, C & D
Target: Secondary, Marshaling Yard at Hanover, Germany
Aircraft Airborne: 34 and 4 PFF
Navigation: The route flown was essentially as briefed to the
Pre-IP. At this point 13A and 13C echelons to the left in order to
obtain the proper interval for the bomb run. The peel off was made at
the IP and individual H2X runs were started on the secondary target.
Bombing altitude was reached at Control Point # 1, 54 minutes prior to
the IP.
Weather: In the target area there were 7/10 strato-cumulus in large
solid patches below 10,000. There were also traces of medium clouds
below 20,000 and some scattered cirrus above 20,000. Weather conditions
at the base on return necessitated an instrument approach by all the
planes. This added considerable time to the mission as holding was
required.
Bombing: After the IP, the Radar Navigator took over and proceeded to
set up course picking up the target at 36 miles. The bombardier was able
to give assistance for course as breaks through clouds made pin-point
pilotage possible. . . . rate checks beyond the 3rd check were not given
by the Radar Navigator. The bombardier determined rate to be good enough
for release. Altitude was 25,000 feet.
Mar 29, 1945
Century Bombers, by Richard Le Strange (assisted by Jim Brown)
denotes that on the 29th the "Still Maghotus" ran dry and the owners
(Capt. Scharding & Lt. Krinke) decided to let it stay dry. . . . . .
There were no air operations.
Mar 30, 1945
Captain John H. Williams led the 100th and the 13th Combat Wing to
Hamburg, Germany to attack the Voss and Bloss Works.
349th
Squadron
Crew joined the 100th on 23 Aug 44 |
|
SGT STEPHEN J. MAJCHRZAK |
ROG |
| LT JOHN H.
WILLIAMS |
P |
SGT DON O. R. SELLWOOD |
TTE |
LT ARTHUR
G. LARSON, JR.
(KIA 31 Mar 45 Zeitz) |
CP |
SGT WILLARD
P. BOSTROM
(KIA 31 Mar 45 Zeitz) |
BTG |
| LT JACK E.
WILD |
NAV |
SGT AUGUST J. KOCIOLEK |
WG |
| LT JOSEPH
J. ORENDORF |
BOM |
SGT JOHN J. OBUCHOWSKI |
WG |
| |
|
SGT GEORGE
E. SLAWIK |
TG |
Flew nine missions a "regular" crew and 20 missions as a Pathfinder
Crew. When named a PFF crew (4 Dec 44), Art Larsen & Will Bostrom were
removed form the crew, Larsen to take over his own crew and since the
BTG was not carried on the PFF aircraft Bostrom went with Larsen. Both
were KIA the last day of March 1945 at Zeitz.
Crew left the U. S. from Camp Kilmer, N. J. aboard the S. S. Brazil &
ten days later docked in Liverpool, Eng. Returning to states, left South
Hampton, Eng on V. E. Day, aboard the USS Kingfisher bound for Boston.
There were no losses and all aircraft attacked.
Tactical Report from 13th CBW
13A Group = 100th A, B, C & D
Target: Secondary, Marshaling Yard at Hanover, Germany
Aircraft Airborne: 34 and 4 PFF
Target: Primary - Engine Erecting Shop of the Vohn and Bloss Works, 5
miles SW of the center of Hamburg, Germany.
Navigation: The route was flown essentially as briefed to the IP.
Bombing altitude was reached 15 minutes prior to the IP. 13A was forced
to overshoot the IP by four miles because of interference from the 487th
Group. Individual H2X runs were started on the primary target.
Weather: Enroute to the target there were 2-3/10 cumulus increasing
to 5-7/10 below 8,000, and nil-2/10 cirrus from 20 to 25,000 increasing
to 57/10 in the target area.
Bombing: 100th "A" - After the turn a the IP, the Radar Navigator
picked up the target and proceeded set the course. The Bombardier was
clutched in at 11 miles and subsequent checks of 10, 9, 8, and 7 miles
were completed. After the seven mile check the formation broke out of
the weather. and the bombardier was able to pick out the target which
was considerably off to the right of course. The bombardier altered
course to the right 30° and positioned the cross hairs on the smoke and
haze that covered the MPI, by using check points out side the target.
Only a few seconds were allowed for synchronization before the BRI (Bomb
Release Line). H2X operated successfully the entire route.
PI Report 100 "A" - No bursts of any bombs dropped by the 100th "A"
were visible. According to computations based on the bomb trajectory
charts and the location of the smoke bombs in the last picture of the
camera sorties, the bombs probably fell in th water and fields one and
one half SW (short) of the primary target.
PI Report 100 "B" - The only set of pictures taken by 100 "B" show
10/10 undercast. Photographs taken by 100 "C" show as squadron's
pattern, which in all probability is that of 100 "B", in the water and
on the Oil Refinery of Europaische Teaklager Transport, A. G. , which is
two and three quarter miles W (left) of the primary. No fires were
started but the main concentration of bombs fell on portions of the oil
installation. Smoke prevented any detailed interpretation of the bomb
pattern.
PI Report 100 "C" - The bombs of 100 "C" fell in a concentrated
industrial area four and three quarters miles WNW (left) of the primary
target.
PI Report 100 "D" - No bursts of any bombs dropped by the 100th "C"
were visible. According to computations based on the bomb trajectory
charts and the location of the smoke bombs in the last picture of the
camera sorties, the bombs probably fell about 3/4 mile S (right) of the
MPI in the water and on a dock area.
Mar 31, 1945
The 100th took off in four groups for the synthetic oil plants at
Zeitz as the primary and Bad Berken as the secondary. The Group lost one
plane piloted by Lt. Arthur G. Larsen, there was one survivor, the Tail
Gunner S/Sgt John E. Kiaser.
44-6470 349th Squadron
MACR#13714, Microfiche#5010 |
|
T/SGT
JOSEPH M. POPSON
(KIA 21 Mar 45) |
ROG |
1ST LT
ARTHUR G. LARSEN
(KIA 21 Mar 45) |
P |
T/SGT
RAYMOND R. BAZATA
(KIA 21 Mar 45) |
TTE |
1ST LT
THOMAS E. O'NEIL
(KIA 21 Mar 45) |
CP |
S/SGT
WILLARD P. BOSTROM
(KIA 21 Mar 45) |
BTG |
2ND LT DALE
F. WATERSON
(KIA 21 Mar 45) |
NAV |
S/SGT
MARVIN F. BARNER
(KIA 21 Mar 45) |
WG |
T/SGT
CHARLES M. DINEEN
(KIA 21 Mar 45) |
TOG |
S/SGT JOHN
E. KAISER
(POW 21 Mar 45) |
TG |
EYEWITNESS: " A/C 44-6470 was hit by flak immediately after bombs
away. #3 engine was knocked loose and dropped off the wing. The A/C
nosed up hen leveled off and started for the undercast in a steep glide.
At the Rally point pilot made a 180 degree turn and headed back
toward Russia. He was heard over VHF saying that #4 prop was running
away and that he would attempt to reach the Russian lines. The A/C was
under control and there was no fire. One chute was seen to leave the
A/C. Allied fighters were escorting A/C. "
STATEMENT OF S/SGT. JOHN E. KAISER. JR. 18243028
The following information was received by Captain Charles W. Terry,
Station 139 Prisoner of War Officer on interrogation of S/Sgt. Kaiser 24
April 1945. S/Sgt Kaiser, since this date has returned to the Zone of
Interior.
"On 31 March 1945,A/C 44-6470 was hit by flak while over the
target at Zeitz, Germany and its #3 engine was knocked out of its
mount. It nosed up out of the formation, leveled off, then started
down in a steep glide. Just before reaching the undercast, the pilot
was heard to say he would try to reach the Russian lines and the A/C
went into the undercast on an easterly heading. "
S/Sgt Kaiser was flying as tail gunner and states that his A/C was
hit twice. After the first hit it remained in level flight and the
engineer called on inter-phone to ask if he was all right. There were
noises from the front that sounded like pieces of the plane were ripping
away. When it was hit again a few seconds later, the A/C started down in
a steep glide. He fastened on his chute and called over in interphone
but no one answered. He looked back into the waist but could see nothing
because of smoke. The A/C was vibrating badly so he decided to get out.
His clothing hung on the handle of the escape hatch and he was trapped
there for about 30 seconds. He tried to climb back into the A/C but was
weak from lack of oxygen and could not, so he pulled his-self up as far
as possible and let go. This freed him from the plane so he opened his
chute and looked down. He floated across the German Air Field located at
5059 N 1231 E. As he floated over the woods just east of this A/F,he
noticed that there were hundreds of E/A dispersed there. He landed in an
open field just east of the woods and was momentarily unconscious. When
he came to, he saw several soldiers (Luftwaffe) approaching, so he stood
up with his hands over his head.
After being captured and brought to a Prisoner of War Camp at Weimer
he was interrogated by a German Officer. The interrogator asked him the
names of the members of his crew. He gave him their last names end was
told that his crew had crashed a few miles away and all had been killed.
As proof he produced a basket containing the dog tags, bill folds,
watches, and other personal property of the men. Sgt. Kaiser was allowed
to look through this equipment and when he found the wedd-ing ring of
his Pilot, 1st Lt Arthur G. Larson, Jr. he asked the Interrogator if he
would not allow him to take it to Lt. Larsen's wife. He replied ''sure"
and gave it to him.
Tactical Report from 13CBW.
100th Group - 100A, B, C, and D Squadrons.
Target: Zietz and Bad Berka (Erfurt), Germany - Primary and
Secondary.
Aircraft Airborne: 34 plus 4 PFF. All aircraft attacked and there
were no losses.
Navigation: Enroute to Control Point #3, 13A was forced to parallel
course 8-10 miles to the south because and unidentified group was
echelon to the left. The route from Control Point #3 was closely
followed until shortly before the IP. At this point the Wing fanned out
and peeled off on individual runs on the primary target. 100A did not
release it's bombs on the primary and attacked the secondary.
Weather: 8 to 10/10 undercast in the target area.
Bombing: 100B- The Radar Navigator assisted in setting up course at
the beginning of the run. The 1st priority target was attacked by the
method of Grid Bombing because very extensive smoke screens covered the
target area. Three miles from the RL (Release Line), however, the target
outline could be seen, but the M. P. I could not be identified. H2X
equipment operated satisfactorily. PI reports no bomb bursts visible,
but according to computations based upon the bomb trajectory chart, the
bombs probably fell in fields 7500' east (right) of the assigned MPI.
The 418th Squadron Diary of March 31 indicates eight 418th aircraft
flew in the "C" Squadron to attack Zeitz. Results were poor for the
synthetic oil target and apparently the crews were not satisfied with
the mission.
April 1, 1945
Vernon Sheedy notes that they day is Easter Sunday and many of the
100th personnel went to church. There were no air operations and he
notes that is was also April Fool's Day.
April 2, 1945
The base personnel were restricted from in country travel between
March 29 and April 4th due to British holidays. This was to make more
public transportation available to British Nationals. It is also noted
that the clocks were moved forward one hour -- beginning of British
Double Summer Time. Lt. Krinke (Harold Krinke), the 100th's man of many
talents, was appointed Advisement Officer.
April 3, 1945
The 100th took off at 1345 hours British Double Summer Time with the
sub yards at Kiel as the target. Bombing was at 1744 hours - most of the
aircraft carried six 1000 pound bombs which were dropped through the
undercast by H2X. Results were said to have not been good.
As the formation approached 54°05'N & 06°20'E, the B-17G (43-38992),
flown by William Baldwin, flying in place of the regular first pilot,
Robert Fletcher (wounded on the March 18th Berlin mission) left the
formation and attempted to return alone. This after Baldwin reported on
VHF that he was low on fuel. The aircraft was never heard from again and
of the ten men aboard all but two perished.
|
43-38992 351st Squadron Crew joined the 100th on
4 Mar 45 (**see note below) |
MACR
#13717 |
SGT KERMIT
E. JONES
(POW 3 Apr 45) |
ROG |
2ND LT
WILLIAN E. BALDWIN, JR.
(KIA 3 Apr 45) |
P |
SGT KENNETH
E. WRIGHT
(KIA 3 Apr 45) |
TTE |
2ND LT
FRANCIS G. BEEDLE
(KIA 3 Apr 45) |
CP |
SGT
RANDOLPH A. GOODWIN
(KIA 3 Apr 45) |
BTG |
F/O JOHN H.
BUCKLEY
(KIA 3 Apr 45) |
NAV |
SGT ALFRED
MANTOPOLI
(KIA 3 Apr 45) |
WG |
SGT LESLIE
O. DAVIS
(KIA 3 Apr 45) |
TOG |
SGT OGDEN
W. BARRON
(KIA 3 Apr 45) |
TG |
| |
|
S/SGT
HOWARD O. WEBER
(POW 3 Apr 45) |
RAD/
CON
|
**This crew, with Robert C. Fletcher as pilot, joined the 100th GP on
4/3/45. Apparently Baldwin took over as P. Francis Beedle had been the
CP on the crew of R. C. Ellis. Howard Weber was not a member of the
original crew.
Eyewitness report had following to say: "A/C #992 was unable to
release bombs over target and retained them until formation reached
5417-0600E on return route. Bombs were then released. The A/C appeared
to be undamaged and continued on with the formation to 5405-0620E at
1850 hours when wheels were lowered and pilot called over VHF saying he
was low on gas and would try to get back alone. The A/C peeled off and
down toward the undercast. When the formation reached 5250-0300E at 1952
hours, a VHF message from A/C 992 was received saying that 80 gallons of
gas per engine was left and the A/C was an estimated 15 minutes from
land. Nothing further was heard. Other pilots suggest that cloud
conditions were favorable for icing and that A/C may have been lost due
to ice picked up in passing through clouds. "
Letter from Kermit E. Jones 17/6/82.
Actually, icing was not the problem as Kermit Jones explains. "We
were returning from Kiel when it was discovered we were running out of
gas so we headed for Belgium. While enroute, and over the first Frisian
Island off the Peninsula of Holland, at an altitude of 5000 feet, we
were hit by flak which destroyed two engines and set the ship on fire. "
According to Jones, he, Goodwin and Wright bailed out but the others
did not and the A/C exploded upon hitting the ground. Jones adds that,
"Sgt. Goodwin landed on the island (Texel) and shed his chute and
flying boots. These were later shown to us by the Germans with a comment
that Sgt. Goodwin was dead. The Germans at the same time showed us the
seven pairs of twisted and burned dog tags of remaining members of the
crew with a statement that they were all dead. "
Of considerable interest in connection with the loss of this crew is
a letter from "The Mayor of Texel" dated 11 Feb. 1946 and apparently
directed to someone who had inquired about the burial of Sgt Barron.
"In answer to your letter of 5 February, we can assure you that
the grave of Sgt. Ogden N. Barron indeed is known.
The plane was shot down on April 3. 1945 at 20 hours (8 p. m. )
and fell near Horntge in the southern part of Textel Island. The
plane had possibly a crew of seven men. Two persons, their names not
known, (they were Jones & Weber) were taken prisoner by the Germans.
The bodies of two persons, namely, Sgt Ogden W. Barron number
420C0553 and Sgt. Randolph Goodwin, number 39855835 were identified.
These two people died instantly when the plane struck the ground.
Also, two others occupants who tried to leave the plane by parachute
were killed instantly on account of the Plane being too close to the
ground. Their names are not known. The possibly seventh occupant has
never been found, either he fell into the sea or was obliterated
under the plane when it fell down.
The bodies of the four crew members were buried on April 10/1945
in the Allied cemetery of the town Den Burg at Textel Island. The
funeral services were somewhat delayed on account of a general
uprising amongst the people with many things abnormal for a few
days. The graves were marked with a wooden cross. On Dec. 7,1945 the
American Graves Registration Command recovered the bodies of the
American boys and reburied them in the American cemetery "Margraten"
in the province of Limburg. "
In two quite touching letters written by one A. van Dienst, an
official of Den Burg, to the mother of John Buckley 30/5/46 and
25/11/46) he attempts to solace Mrs. Buckley and, at the same time,
explain the difficulties met with in identifying the airmen who perished
in the crash.
"Parts of different bodies were found, namely two bodies and four
pair of hands, partly burnt, found in or near the plane. These were
buried in one coffin at 10 April in the war cemetery of Den Burg
about 20 meters from my house. "
van Dienst then proposes the possibility that some human remains, if
not consumed by fire, might still be in "parts of the plane that are
pushed deep into the ground". He further promises to attempt to interest
the American Graves Registration in digging up the buried aircraft to
search for any remains.
In the letter of 25/11/46, van Dienst writes Mrs. Buckley that Graves
Registration had further examined the wreckage and had been able to
identify remains of William E. Baldwin, Francis G. Beedle, Sgt Alfred
Mantopoli and Kenneth Wright.
Thus we know that F/O John Buckley and Sgt Leslie O,Davis were the
two unidentified crewmen "buried in one coffin" on 10 April 1945. van
Dienst concludes his letter to Mrs. Buckley by saying that the cross
marking this grave reads "Unknown American Flyers" but the rear side of
the cross now says, "Probably, F/O John H. Buckley and Sgt Leslie O.
Davis".
----------------------------------------Paul West-------------------------------------
|